Airborne Express Flight 827

{{Short description|1996 airplane crash}}

{{use mdy dates|date = September 2019}}

{{use American English|date = September 2019}}

{{Infobox aircraft occurrence

| image = McDonnell Douglas DC-8-61(F), Airborne Express AN0213062.jpg

| image_upright = 1.15

| alt =

| caption = N851AX, An Airborne Express DC-8 similar to the aircraft involved

| occurrence_type = Accident

| date = {{start date|1996|12|22}}

| summary = Failed stall recovery test; pilot error

| site = Narrows, Virginia, United States

| coordinates = {{Coord|37|19.30|N|80|53.06|W|type:event_region:US-VA|display=inline,title}}

| aircraft_type = Douglas DC-8-63F

| aircraft_name =

| operator = ABX Air under Airborne Express

| IATA = GB827

| ICAO = ABX827

| callsign = ABEX 827

| tail_number = {{Airreg|N|827AX}}

| origin = Piedmont Triad International Airport, Greensboro, North Carolina

| stopover =

| stopover0 =

| last_stopover =

| destination = Piedmont Triad International Airport, Greensboro, North Carolina (Return flight)

| occupants = 6

| passengers = 3

| crew = 3

| fatalities = 6

| injuries =

| missing =

| survivors = 0

}}

Airborne Express Flight 827 was a functional evaluation flight (FEF) of an ABX Air (under Airborne Express) Douglas DC-8-63F (registration N827AX) that had undergone a major modification. On December 22, 1996, during the test flight, the aircraft stalled and crashed, killing all six people on board. Accident investigators determined the cause of the accident was improper crew control inputs.{{Cite web |date=July 15, 1997 |title=Uncontrolled Flight into Terrain, ABX Air (Airborne Express), Douglas DC-8-63, N827AX, Narrows, Virginia, December 22, 1996 |url=https://www.ntsb.gov/investigations/AccidentReports/Reports/AAR9705.pdf |access-date=September 5, 2019 |publisher=National Transportation Safety Board |id=NTSB/AAR-97/05}}{{cite web |last=Ranter |first=Harro |title=Accident description |url=http://aviation-safety.net/database/record.php?id=19961222-0 |access-date=24 February 2010 |website=Aviation Safety Network |publisher=Flight Safety Foundation}}

Background

= Aircraft =

File:Douglas DC-8-63, Capitol Air AN1002638.jpg as a passenger aircraft]]

The aircraft involved was a Douglas DC-8-63 freighter registered as N827AX. The aircraft had been built in 1967 and was previously owned by KLM as a passenger aircraft (with registration PH-DEB) and then Capitol Air and National Airlines (registration N929R). In January 1986 the aircraft was converted into a freighter and delivered to Emery Worldwide (with the same registration). ABX Air (a subsidiary of Airborne Express at the time) purchased the aircraft on June 17, 1996, more than six months before the accident. The aircraft was re-registered as N827AX. It underwent a major overhaul and was delivered to ABX Air on December 15 the same year, just a week before the accident. The aircraft was powered by four Pratt & Whitney JT3D-7 turbofan engines. At the time of the accident, the aircraft had flown 62,800 hours and nine minutes with 24,234 take off and landing cycles.{{Reference page|page=7}}{{Cite web |title=N827AX Airborne Express Douglas DC-8-60/70 |url=https://www.planespotters.net/airframe/douglas-dc-8-n827ax-airborne-express/ey1vg5 |access-date=2019-12-16 |website=www.planespotters.net|date=October 11, 2019 }}{{Cite web |title=Registration Details For N827AX (ABX Air) DC-8-63 |url=https://www.planelogger.com/Aircraft/Registration/N827AX/648697 |access-date=2019-12-19 |website=www.planelogger.com}}

== Overhaul ==

The aircraft's overhaul was performed by the Triad International Maintenance Corporation (TIMCO) at Piedmont Triad International Airport in Greensboro, North Carolina.{{Reference page|page=1}} During the major overhaul, the aircraft received major avionic upgrades, including the installation of an electronic flight instrument system (EFIS). All four engines were removed. Two of them were overhauled and reinstalled on the aircraft, while the other two were completely replaced by different JT3D-7 engines from ABX Air. Hush kits were installed on all of the engines for noise reduction. The aircraft's stall warning system was tested and declared functional.{{Reference page|pages=7–8}}

= Crew =

Rather than a captain, a first officer and a flight engineer, Flight 827 was crewed by two captains (one flying, one monitoring), and a flight engineer. There were also three aircraft technicians on board.{{Reference page|page=4}}

The captain who was the pilot monitoring (though acting as pilot in command (PIC)) was 48-year-old Garth Avery, who had worked for Airborne Express since 1988 and had 8,087 flight hours, including 869 hours on the DC-8. He was seated in the right seat. Avery was also the airline's Boeing 767 flight manager as well as a flight instructor.{{Reference page|pages=4–5}}{{Cite news |last= |first= |date=1996-12-23 |title=CARGO PLANE CRASHES, KILLING SIX |work=Clearfield Progress |agency=Associated Press |url=http://www.gendisasters.com/virginia/18940/narrows-va-dc-8-cargo-plane-crashes-dec-1996 |url-status=dead |access-date=2019-10-25 |archive-url=https://web.archive.org/web/20191025234307/http://www.gendisasters.com/virginia/18940/narrows-va-dc-8-cargo-plane-crashes-dec-1996 |archive-date=October 25, 2019 |via=GenDisasters}}

The captain who was the pilot flying (though acting as a co-pilot) was 37-year-old William "Keith" Leming, who had worked for Airborne Express since 1991 and had logged 8,426 flight hours, with 1,509 of them on the DC-8. He was seated in the left seat. Leming was the manager of Airborne Express' DC-8 flight standards (the position previously having been held by Captain Avery) and had previously been a pilot for Trans World Airlines.{{Reference page|pages=2,5}}{{Cite news |last=Clothier |first=Mark |date=1996-12-25 |title=DC-8 CRASH MARS HOLIDAY PROBE ON HOLD; FAMILIES MOURN |website=The Roanoke Times |url=https://scholar.lib.vt.edu/VA-news/ROA-Times/issues/1996/rt9612/961225/12260047.htm |access-date=2020-05-22}}

The flight engineer was 52-year-old Terry Waelti who, like Captain Avery, had been with Airborne Express since 1988. Waelti had 7,928 flight hours, including 2,576 hours on the DC-8. He was also a DC-8 examiner designated by the Federal Aviation Administration (FAA). Waelti had previously served in the United States Air Force (USAF) and was one of the USAF's first flight engineers to be qualified on the Boeing E-4B.{{Reference page|pages=5–6}}{{Cite news |date=1996-12-29 |title=PAID OBITUARES |work=Sun-Sentinel |url=https://www.sun-sentinel.com/news/fl-xpm-1996-12-29-9612290115-story.html |url-access=subscription |access-date=2020-05-22}}

The three technicians were 48-year-old Edward Bruce Goettsch, 39-year-old Kenneth Athey, and 36-year-old Brian C. Scully. Goettsch and Athey both worked for Airborne Express, while Scully worked for TIMCO.{{Cite news|url=https://www.greensboro.com/families-grieve-for-victims-of-plane-crash/article_d2137378-120c-5b0b-9a29-669615999e5b.html|title=FAMILIES GRIEVE FOR VICTIMS OF PLANE CRASH|last1=Newsom|first1=John|date=1996-12-23|work=News and Record|access-date=2019-10-28|last2=Krouse|first2=Peter}}

Accident

Initially, Flight 827 had been scheduled to depart from Piedmont Triad International Airport on December 16, but was delayed due to maintenance. An attempt on December 21, (operated by the same crew) was cut short due to a hydraulic problem. Flight 827 finally departed at 17:40 Eastern Standard Time (EST) at nighttime on December 22, 1996, after being delayed due to additional maintenance. The flight climbed to {{Convert|9000|ft|m|abbr=}} and then to {{Convert|14000|ft|m|abbr=}}.{{Reference page|page=1–2}}

Flight 827 was operating under instrument flight rules (IFR). After departing Greensboro, the aircraft was to fly northwest over New River Valley Airport's VOR, in Pulaski County, Virginia, then to Beckley, West Virginia, followed by other way points in Kentucky and Virginia, and then return to Greensboro. The flight was expected to last two hours.{{Reference page|page=2}}

Shortly after reaching {{Convert|14000|ft|m|abbr=}}, the aircraft experienced atmospheric icing, which was indicated when the cockpit voice recorder (CVR) recorded captain Lemming saying, "we're gettin' a little bit of ice here," and "probably get out of this," at 17:48:34 and 17:48:37 respectively.{{Reference page|page=2}}

Several landing gear, hydraulic, and engine tests were performed without incident. At 18:05, flight engineer Waelti said, "next thing is our stall series." The next item was a clean stall maneuver test. The crew would slow the aircraft down until the stick shaker activated, record the stall speed and that of the stick shaker activation, and then recover control of the aircraft. In other words, the flight crew would deliberately stall the aircraft.{{Cite journal |date=September 1997 |title=After Intentionally Stalling DC-8, Crew Uses Incorrect Recovery Technique, Resulting in Uncontrolled Descent and Collision with Terrain |url=https://flightsafety.org/ap/ap_sept97.pdf |journal=Accident Prevention |location=Alexandria, VA |publisher=Flight Safety Foundation |volume=54 |issue=9}} Captain Avery stated that the crew would stop trimming the aircraft at {{Convert|184|kn|mph km/h|abbr=}} and that the stall speed (VS) was {{Convert|122|kn|mph km/h|abbr=}}. Flight engineer Waelti stated that the stick shaker would activate at {{Convert|128|kn|mph km/h|abbr=}}, which was {{Convert|6|kn|mph km/h|abbr=}} higher than the calculated stall speed. The flight crew began gradually slowing the aircraft down by {{Convert|1|kn|mph km/h|abbr=}} per second.{{Reference page|page=2}}

At 18:07, engine power was increased. One minute later at 18:08, a buffeting sensation was experienced at {{Convert|149|kn|mph km/h|abbr=}}.{{Reference page|page=12}} The following was recorded on the CVR:{{Cite news |last=Schmid |first=Randolph E. |date=1997-03-26 |title=Cargo crash occurred during routine stall tests, documents show |work=Associated Press |url=https://apnews.com/1e743ab88625550c72d5187b93291d82 |url-status=dead |access-date=2020-05-22 |archive-url=https://web.archive.org/web/20230207233554/https://apnews.com/article/1e743ab88625550c72d5187b93291d82 |archive-date=2023-02-07}}

align="center" cellpadding="1" style="border:none;"

! style="width:6.0em;" |

! style="width:10.0em;" |

! style="width:37.0em;" |

style="vertical-align:top;"

|18:07:55

|Commentary

|Sound similar to engine increasing in RPM.

style="vertical-align:top;"

|18:08:06

|Captain Lemming

|Some buffet.{{Efn|At the time of this comment, the aircraft's speed was {{Convert|240|kn|mph km/h|abbr=}}.{{Reference page|page=3}}}}

style="vertical-align:top;"

|18:08:07

|Captain Avery

|Yeah. That's pretty early. *.{{Efn|The NTSB uses an asterisk to indicate unintelligible words in CVR transcripts.{{Reference page|pages=34,56}}}}

style="vertical-align:top;"

|18:08:09

|Commentary

|Sound of rattling.

style="vertical-align:top;"

|18:08:11

|Flight Engineer Waelti

|That's a stall right there… * ain't no [stick] shaker.

At this time, according to the flight data recorder (FDR), the aircraft was at {{Convert|145|kn|mph km/h|abbr=}}.{{Reference page|page=3}} However, the stick shaker had failed to activate.{{Reference page|page=36}} The speed then decreased to {{Convert|126|kn|mph km/h|abbr=}} and the aircraft entered a real stall.{{Reference page|page=11}} At 18:08:13, captain Lemming decided to terminate the test, called "set max power," and applied full engine power in an attempt to recover from the stall.{{Reference page|page=36}} Although all four engines started to accelerate, engine no. 2 accelerated more slowly.{{Reference page|page=11}} This engine subsequently experienced a compressor stall.{{Reference page|pages=12,95}} Ground witnesses also noted that the aircraft was making "skipping or missing" sounds.{{Reference page|page=3}} At 18:09, Air Traffic Control (ATC) asked the flight if they had initiated an emergency descent, with captain Avery replying, "yes sir." This was the last communication (and only distress call) from Flight 827.{{Reference page|page=3}}

At 18:09:35, the ground proximity warning system (GPWS) activated and sounded "terrain terrain, whoop whoop pull up." Three seconds later at 18:09:38, the aircraft crashed into a mountain travelling over {{Convert|240|kn|mph km/h|abbr=}} in a nose-down wings-down position of 26 and 52 degrees, respectively. The crash site elevation was {{Convert|3400|ft|m}} mean sea level (MSL).{{Reference page|pages=3,12}} The aircraft exploded on impact.{{Cite news |last1=Kelley |first1=Brian |last2=Hayden |first2=Betty |date=1996-12-23 |title=PLANE CRASH KILLS 6 NONE ON CARGO JET SURVIVE |edition=Metro |pages=A1 |website=The Roanoke Times |url=https://scholar.lib.vt.edu/VA-news/ROA-Times/issues/1996/rt9612/961223/12230105.htm |access-date=2023-11-25 |via=Virginia Tech}} All six people on board were killed and the aircraft was destroyed.{{Reference page|pages=3–4}}

Investigation

The National Transportation Safety Board (NTSB) launched an investigation into the accident and arrived at the crash site the same day.{{Reference page|page=55}} Both flight recorders were recovered the next morning.{{Reference page|page=55}}{{Cite news |last=Pae |first=Peter |date=1996-12-24 |title=RECORDERS FOUND IN AIR CRASH |newspaper=The Washington Post |url=https://www.washingtonpost.com/archive/local/1996/12/24/recorders-found-in-air-crash/62d29e2e-8dec-479b-ad14-0619ac7c8ee2/ |access-date=2019-10-25}}{{Cite news |last=Reed |first=David |date=1996-12-24 |title=NTSB: Pilot radioed distress call before cargo plane crash |url=https://apnews.com/af59da6bdbe3ea6df87d81e86b54567e |url-status=dead |archive-url=https://web.archive.org/web/20191218014737/https://apnews.com/af59da6bdbe3ea6df87d81e86b54567e |archive-date=2019-12-18 |access-date=2019-12-18 |work=Associated Press}} Rescue teams also recovered all six bodies.{{Cite news |last=Reed |first=David |date=1996-12-23 |title=Cargo plane pilot makes distress call moments before crash |work=Associated Press |url=https://apnews.com/8c01d7d9930d44b9853ae4c2e72e430b |url-status=dead |access-date=2020-02-24 |archive-url=https://web.archive.org/web/20200224231539/https://apnews.com/8c01d7d9930d44b9853ae4c2e72e430b |archive-date=2020-02-24}} Efforts to reach the accident site were initially hampered due to its remote location.{{Cite news |last=Reed |first=David |date=1996-12-22 |title=Plane crashes in Virginia forest |work=Associated Press |url=https://apnews.com/f57eb01b45a1bdd3df50166f255e5fdb |url-status=dead |access-date=2019-10-25 |archive-url=https://web.archive.org/web/20191025234309/https://apnews.com/f57eb01b45a1bdd3df50166f255e5fdb |archive-date=2019-10-25}}

The aircraft's flight controls were destroyed in the crash, but the NTSB recovered two trim jackscrews from the horizontal stabilizer.{{Reference page|page=13}}

The NTSB recreated the stall in a simulator. In the simulation, the stick shaker activated at {{Convert|144|kn|mph km/h|abbr=}}. Despite deepening the stall, no unexpected nose-down pitches or lateral rolls occurred in the simulator. The decreasing airspeed caused the nose to pitch up.{{Reference page|page=14}}

In 1991, another Airborne Express DC-8 had entered a real stall during an FEF, but the flight crew was able to recover and test continued with no further incidents. In the 1991 incident, the stick-shaker activated the same time the buffeting sensation occurred. The Federal Aviation Administration (FAA) issued a revised stall recovery procedure to Airborne Express, which they agreed to incorporate. However, the airline had only partially incorporated the procedure at the time of the Flight 827 accident.{{Reference page|page=21}}

Airborne Express' flight operation manual contained only a short section labeled "Test Flights" and the requirements for FEF's read:

{{Blockquote|text=...night test flights may be conducted only when the reported ceiling is 800 feet or above and the reported visibility is 2 miles or greater, and the weather forecast indicates that the ceiling and visibility will remain at or above those limits for the duration of the flight. Night test flights flown by flight supervisory personnel may be operated with lower minimums when circumstances warrant.{{Reference page|page=22}}|author=Airborne Express|title=Flight Operations Manual}}

At the time of the accident, there were scattered showers of light rain and the cloud ceiling was between {{Convert|14000|ft|m|abbr=}} and {{Convert|15000|ft|m|abbr=}}. The reported surface weather at Mercer County Airport in Bluefield stated that visibility was two miles.{{Reference page|page=10}}

Because of the aircraft experiencing icing, it experienced a buffet {{Convert|12|kn|mph km/h|abbr=}} before the stall speed. The FDR indicated that the aircraft had entered a real stall at {{Convert|126|kn|mph km/h|abbr=}}, four knots before the stall speed. The NTSB concluding that the icing, regardless of amount, (along with flight control rigging) did not contribute to the accident.{{Reference page|pages=32–34}}

Despite Captain Lemming's timely decision to terminate the stall test, he subsequently pulled back on the control column from five to ten degrees, allowing the aircraft to enter a real stall.{{Reference page|page=32}} The NTSB notes that he likely did this in an attempt to establish an appropriate pitch attitude and power setting.{{Reference page|page=32}}

Captain Avery did not notice the incorrect flight control inputs made by captain Lemming, though he did attempt to instruct Lemming on to recover the airplane from the roll, but not how to recover from the stall. In addition he did not enhance his instructions or take over control of the aircraft himself. The NTSB noted that since both pilots were captains, had manager positions at the airline, and had similar backgrounds, they would have difficulty challenging each other because of a lack of command authority.{{Reference page|page=35}} Captain Avery, as PIC, should have monitored and challenged captain Lemming's actions, but both his PIC and instructional roles were informal on the accident flight.{{Reference page|pages=35–36}}

According to both flight recorders and the recovered horizontal stabilizer trim jackscrew, captain Lemming had trimmed the aircraft's horizontal stabilizer at {{Convert|175|kn|mph km/h|abbr=}} instead of the intended {{Convert|184|kn|mph km/h|abbr=}}. Airborne Express' procedures required the aircraft to be trimmed {{Convert|1.5|kn|mph km/h|abbr=}} before the stall speed. Despite the incorrect trim setting, the aircraft would still have been recoverable from the stall. The NTSB concluded that the captain Lemming's incorrect trimming of the horizontal stabilizer was not a factor in the accident.{{Reference page|page=34}}

The NTSB examined N827AX's maintenance records and reviewed Airborne Express' procedures for testing the stall warning system, but could not determine why the stick shaker was inoperative during the accident flight.{{Reference page|pages=36–37}} In addition, the flight crew's situational awareness that the aircraft was in a stall was short, as they were distracted by the compressor stall on the no. 2 engine and communications with ATC. The NTSB also stated that an angle of attack display on the flight deck could have helped the crew situational awareness. The fact that the crew lacked a visual horizon at nighttime was another factor due to the aircraft being in instrument meteorological conditions (IMC) from the time the stall maneuver was performed until impact.{{Reference page|pages=36–39}}

Neither captain Avery nor captain Lemming had ever flown a DC-8 post modification on an FEF until December 21 (the initial FEF that was aborted), though the director of flight technical programs authorized Avery to serve as a pilot in command on post modification FEF's.{{Reference page|pages=44–46}}

= Final report =

The NTSB released the final report on July 15, 1997. The "probable cause" section stated the following:

{{Blockquote|text=The National Transportation Safety Board determines that the probable causes of this accident were the inappropriate control inputs applied by the flying pilot during a stall recovery attempt, the failure of the nonflying pilot-in-command to recognize, address, and correct these inappropriate control inputs, and the failure of ABX to establish a formal functional evaluation flight program that included adequate program guidelines, requirements and pilot training for performance of these flights. Contributing to the causes of the accident were the inoperative stick shaker stall warning system and the ABX DC-8 flight training simulator's inadequate fidelity in reproducing the airplane's stall characteristics.{{Reference page|pages=v,51}}|author=National Transportation Safety Board}}

The accident had been caused by pilot error due to captain Lemming's improper flight control inputs and captain Avery's failure to notice them. Another cause was Airborne Express failing to set up a proper program for FEFs, resulting in inadequate training.{{Cite press release |date=1997-07-15 |title=Pilot mistakes, inadequate Airborne Express training and procedures led to fatal crash of DC-8 cargo plane |url=https://www.ntsb.gov/news/press-releases/Pages/Pilot_mistakes_inadequate_Airborne_Express_training_and_procedures_led_to_fatal_crash_of_DC-8_cargo_plane.aspx |archive-url=https://web.archive.org/web/20150326023314/https://www.ntsb.gov/news/press-releases/Pages/Pilot_mistakes_inadequate_Airborne_Express_training_and_procedures_led_to_fatal_crash_of_DC-8_cargo_plane.aspx |archive-date=2015-03-26 |access-date=2019-12-19 |publisher=National Transportation Safety Board}}{{Cite news|date=1997-07-16|title=PILOT TRAINING FAULTED|newspaper=The Washington Post|url=https://www.washingtonpost.com/archive/local/1997/07/16/pilot-training-faulted/70c1d983-8056-4748-995f-35a81bd5a962/|access-date=2021-02-09|issn=0190-8286}}{{Cite news |last=Krouse |first=Peter |date=1997-07-15 |title=FATAL CRASH BLAMED ON PILOT ERROR / FEDERAL OFFICIALS ALSO SAY AIRBORNE EXPRESS FAILED TO INSTITUTE ADEQUATE TEST-FLIGHT GUIDELINES |work=News and Record |url=https://www.greensboro.com/fatal-crash-blamed-on-pilot-error-federal-officials-also-say/article_d0413a13-1948-5ddc-9233-abaa382acfbc.html |access-date=2020-02-24}} Contributing factors included the stick shaker being inoperative, inaccuracies in Airborne Express' flight simulators when simulating a stall, the compressor stall on the no. 2 engine which distracted the flight crew, the accident occurring at night (which resulted in the flight crew's lack of a visual horizon and other exterior cues), and Airborne Express not requiring flight tests to be completed before nightfall.{{Reference page|pages=49–50}}{{Cite web|last=Schlimm|first=Karl|date=2009-10-13|title=LESSONS LEARNED : DC-8 MISHAP ON 22 DECEMBER 1996|url=https://www.apstraining.com/resource/lessons-learned-dc-8-mishap-on-22-december-1996/|access-date=2020-07-07|website=Aviation Performance Solutions}} Airborne Express agreed with the NTSB that the pilots used incorrect procedures, but disputed two other findings, citing that Avery did have prior experience controlling a DC-8 during a stall, and stated that the revised stall procedures were fully implemented at the time of the accident.

Aftermath

The NTSB issued seven safety recommendations to the FAA. The NTSB also reiterated a previous recommendation regarding the angle of attack following the crash of American Airlines Flight 965 on December 20, 1995:

{{Blockquote|Require that all transport-category aircraft present pilots with angle of attack information in a visual format, and that all air carriers train their pilots to use the information to obtain maximum possible climb performance.{{Reference page|page=27}}{{Cite web|date=1996-10-16|title=Safety Recommendation A-96-094|url=https://www.ntsb.gov/safety/safety-recs/recletters/A96_90_106.pdf|access-date=2019-10-25|publisher=National Transportation Safety Board}}|author=National Transportation Safety Board}}

Lynn Scully, the wife of Brian Scully, filed a lawsuit against Airborne Express for $20 million.{{Cite news |last=Christian |first=Paula |date=1997-07-15 |title=VICTIM'S FAMILY FILES SUIT |work=News and Record |url=https://www.greensboro.com/victim-s-family-files-suit/article_6a2550d1-5c92-52b0-9006-867593a1fcbf.html |access-date=2020-02-24}}

Brian Scully's sister, Maureen DeMarco, was killed in the crash of Comair Flight 3272 on January 9, 1997. Maureen was headed to Brian's funeral.{{Cite news |date=1997-01-10 |title=Colorado teacher killed en route to brother's funeral |work=Associated Press |url=https://apnews.com/article/2ccc58cb117466f1779afb50e8570b79 |url-status=dead |access-date=2022-01-01 |archive-url=https://web.archive.org/web/20230207233930/https://apnews.com/article/2ccc58cb117466f1779afb50e8570b79 |archive-date=2023-02-07}}

Dramatization

This accident was featured in season 25 of Mayday, titled "Fatal Test Flight".{{Cite web |last=TV |first=NatGeo |title=National Geographic - Lentoturmatutkinta |url=https://www.natgeotv.com/fi/ohjelmat/natgeo/lentoturmatutkinta |access-date=2025-01-29 |website=www.natgeotv.com |language=fi}}

See also

Notes

{{notelist}}

References

{{NTSB}}{{Reflist}}